The Partnership: A History of the Apollo-Soyuz Test Project
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
Phase |
S-IB |
S-IVB |
Instrument unit |
---|---|---|---|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
Phase |
CSM 111 |
DM 2 |
DS 5 |
---|---|---|---|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
According to a 1972 "Apollo Experience Report," stress corrosion cracking had been the most common cause of structural-materials failures in the Apollo program. "The frequency of stress-corrosion cracking has been high and the magnitude of the problem, in terms of hardware lost and time and money expended, has been significant."*** 3 Since some of the alloys used in the construction of the Saturn IB launch vehicle were known to be susceptible to stress corrosion, routine inspections had long been a standard procedure. After the discovery in late 1973 of cracks in eight stabilizing fins of the S-IB stage used to launch Skylab 4, the SA 210 fins were given special attention. A crack was first noted on a test fin undergoing a stress corrosion check at the Michoud Assembly Facility, New Orleans. A subsequent, more detailed investigation of all eight fins of SA 210 at KSC on 19 February 1975 discovered cracks in the hold-down fittings in two of the fins.4 In a telex to Professor Bushuyev, Glynn Lunney explained that "this fitting serves no purpose in flight, but supports the launch vehicle on the hold-down arms of the mobile launcher. The critical load on this fitting would occur during 'rebound' if the launch were to be aborted after engines were started and before hold-down arms are released. Fins without cracks have been modified to reduce the stress in the area where cracks initiated. Portions of the fittings were also treated to provide compressive stresses in the surface which also prevents cracking. A fin with these fixes was tested to 142 percent of the design rebound load. Modified fins are now being installed and there is no delay in launch schedule."5 After the replacement of all eight fins, which solved the stress corrosion problem, this issue was certified to have been corrected during the Headquarters Flight Readiness Review, 12 June 1975.6
Table F-3 lists the schedule of events prior to the launch of both Soyuz and Apollo.
Time (EDT) |
Time to launch |
Procedure |
---|---|---|
|
|
|
|
|
|
|
|
|
Time (EDT) |
Time to launch |
Procedure |
---|---|---|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
* These thrust figures are calculated from data made available by the Soviets.
** Both the Saturn IB and its predecessor helped to lay the foundation for the Saturn V program. The Saturn V had three stages - the S-IC, the S-II, and the S-IVB. The Saturn IC had five kerosene and liquid oxygen F-1 engines producing 33.4 million newtons (7.5 million pounds), while the Saturn II stage produced 4.5 million newtons (1 million pounds) with five J- 2 engines. The Saturn IVB was the same stage as used on the S-IB launch vehicle.
*** When certain metal alloys are exposed to a corrosive environment while at the same time they are subjected to an appreciable, continuously maintained, tensile stress, rapid structural failure can occur as a result of stress corrosion. This is known as stress corrosion cracking and is characterized by a brittle-type failure in a material that is otherwise ductile.
1. Reliable data on Soviet launch vehicles are hard to find. This summary is based on the following sources: [Soviet Academy of Sciences], "Apollo-Soyuz Test Project; Information for Press," 1975, pp. 76-78; Charles S. Sheldon II, "The Soviet Space Program Revisited," TRW Space Log (1974), pp. 2-19; Peter L. Smolders, Soviets in Space (Guildford and London, 1973), pp- 62-68; U.S. Congress, Senate, Committee on Aeronautical and Space Sciences, Soviet Space Programs, 1966-70; Staff Report, 92nd Cong., 1st sess. (9 Dec. 1971), pp. 130-132 and 559- 563; and ASTP mission commentary transcript, MC 9/1, 15 July 1975.
2. NASA, MSFC, KSC, et al., "Saturn IB News Reference," Dec. 1965 (changed Sept. 1968); and Ellery B. May to Edward C. Ezell, 24 Feb. 1976, with enclosed data on SA 210.
3. NASA, JSC, Robert E. Johnson, "Apollo Experience Report, the Problem of Stress-corrosion Cracking," TN S-344 (MSC-07201), review copy, July 1972, p. 1.
4. NASA, MSFC, "Design Guidelines for Controlling Stress Corrosion Cracking," 15 June 1970; [Chrysler Corp.], C. C. Davis to R. J. Nuber, memo, "Submittal of CCSSD ECP's EP 12112 and EP 12112T - Additional Structural Components Requiring Stress Corrosion Inspection and Supplemental Test ECP," 10 Jan. 1974; NASA, MSFC, "ASTP Launch Vehicle Stress Corrosion Review," 11 Nov. 1974; R. J. Schwinghammer to Ellery B. May , memo, "Stress Corrosion Assessment of AS-210," 14 Nov. 1974; NASA, MSFC, "ASTP SA-210 Launch Vehicle Design Certification Review," 15 Nov. 1974; and NASA News Release, KSC-27-75, "Two ASTP Saturn IB Fins to Be Replaced," 25 Feb. 1975.
5. TWX, Glynn S. Lunney to Konstantin Davydovich Bushuyev, 17 Mar. 1975.
6. NASA News Release,
MSFC, 75-43, "All Eight Saturn I-B Fins to Be Replaced," 28 Feb.
1975; and NASA, HQ, "Saturn IB Stress Corrosion," General Management
Review Report, 17 Mar. 1975.
Next